Welder repair

An ancient proverb says that power tool failures occur in threes. During the same week that the lathe motor burned out and the compressor wire meltdown has turned it into a scary noise machine, we also had a mysterious malfunction in one of our welders. It didn’t release any smoke, didn’t make weird noises. It just didn’t weld. 0 volts across the output.

Inside of the welder (top view) before the repair attempt. Note that a large number of similar – but not identical – top boards can be found on Aliexpress.

This machine, a small 180A TIG/MMA inverter welder, has recently been repaired. It was not used heavily, as TOG has only so much use for welding. In fact, it was only used by a couple members to practise their welding skills.

On one hand, this machine was 5 year old, has been used extensively in the past and could have been written off as death of old age. The cost of a commercial repair would probably exceed the value of the welder. On the other hand – why not try to repair it ourselves before scrapping it?

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First cuts with TOG’s DIY CNC router

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A few months ago we’ve mentioned a DIY build of a CNC router. The project turned out to be more complicated than we anticipated. The steel-based construction is not very forgiving, and the large size of the machine doesn’t help. Still, due to all the help from many members we managed to overcome a number of difficulties and do a few test engravings in MDF.

MDF is not a difficult material to mill – the most noticeable problems are the awful dust and the fluff around the edges of the cut.  The furry edge is easily fixed using sand paper, but the dust will probably require some more drastic measures in order to protect our lungs. Eventually we’re planning to cut and engrave a variety of materials, many of which have interesting properties but are incompatible with our laser cutter.

Visit us during one of our Monday CAD nights to see the new machine in action or in the video below.

 

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More lathe work

Our lathe is finally getting some good use! This time, a small partHose adapter - work in progress was made from aluminium, a coupling for connecting two pieces of tubing for the water cooling system in the upcoming CNC router project. It will replace the existing temporary hose-and-clamps hack.

A piece of bar stock was clamped in a 4 jaw chuck, made into a
cylinder and turned down to about 16mm diameter. Next we turned half of it down to about 6mm and drilled a 4.5mm hole through it, using a drill chuck. Lastly we smoothed the edges slightly and parted the whole thing off.

The end result is more fIt fits!unctional and looks a lot better!

The whole operation went smoothly in overall retrospection. However, we had few small issues to deal with on the way. Firstly, it wasn’t obvious how to set gearing for the power feed, as the manual wasn’t very clear. Another problem was that the  square shape of stock, required the use of a 4 jaw chuck, which is not self-centring.  That adds a couple of extra steps to set up, as centring of the stock has to be done manually in such a case.